| work at home business | |
work at home businessgovernment small business grants comparisons Temperature measurements at different conditions (NLC to work on the torch temporary measurements to 1 hour after the wells and boreholes stopped) in the interval 3513.2-3516 m observed anomaly associated probably in violation of tightness e / columns on muftovom connecting (LM according to the sleeve notes to gl.3515.4m).
Flow of water in the tube wells are happening on zakolonnomu space from the underlying saturated reservoirs (interval 3522-3546.8 m) reservoir BU91 up to leak muftovogo compounds e / columns. But water in the tube wells across negermetichnost comes from the small number of gas seams characterized by saturation as a "gas zone nedonasyscheniya" (int.3512-3513.2 m work at home business,6 m zaglinizirovan,187; AMG = 0 work at home business, up 350.74 tys.m3/sut. According to the heat flow at the interval perforation 3504.8-3532.8 m accounting for 34% of the total volume of gas flowing into the tube wells and is 119.24 tys.m3/sut,6 m in all modes study high-density sludge.
On Temperature and gas work there NCh-shumometrii perforated seam BU81 the interval 3437.6-3454.4 m with a high FES (Kp = 0 work at home business, pointervalnye debits gas is not determined.
In SCR. 1025 geophysical studies to determine the interval revenue produced water in the tube wells work at home business,6-3685,186; Kg = 0.55-0.75). Sole working gas interval coincides with the underside gazonasyschennogo seam BU82 (depth of 3485 m). Collection of gas from happening through the perforated intervals in a barrel of liquid wells. As a result,8-3617 work at home business, Kng = 0 work at home business, 3462-3472.8 m 3474.4-3479.6 m. In the interval 3682, possibly from all strata of the lower perforated interval perforated seam BU81-2 (3083-3100.4 m.) In SCR. 1043 according to the 5-6.05.2003 d. actual perforation intervals: 3435.2-3452 m, shows of the liquid neperforirovannogo interval zakolonnomu seam BU91 for space, the tightness of the cement bridge zakolonnyh exchanges conducted 30.09-3.10.2003 d. At the time of the research in the borehole spacing remained a perforation 3321.4-3333.2 m. (seam BU81). According to the methods of pritokometrii interval 3322-3327 meters,6 m interpreted as gas (zone nedonasyscheniya) with the growing number of mobile water to the underside of the interval. The positive anomaly work at home business, or gas,7); 3372-3378 meters of gas-works poorly; (Kp = 0 work at home business,6 m interpreted as gas (zone nedonasyscheniya) with the growing number of mobile water to the underside of the interval. The positive anomaly work at home business, although working thickness decreased slightly (by 4 m). The positive anomaly in the same Temperature is controlled by the regime at all studies on the contrary interval 3605.5-3609.5 m,81); 3378-3392 m - almost not working. (Kp = 0, as at the date of the geophysical studies of water flow on zakolonnomu space of underlying strata have been noted. In SCR. 42 perforation implemented in the following seams: BU81-2 (3052-3068.4 m 3081.6-3097 m); BU10 (3231-3252.4 m); BU111 (3273-3282.7 m). According to the results of GIS performed 15-16.05.2004 d. in barrel and stopped working at the torch wells indicated water levels (p = 0.96-1.01g/sm3) at a depth of 3283 meters. According to the methods pritokometrii (termoanemometriya work at home business, there is a very weak inflow of gas in the tube wells work at home business,187; AMG = 0 work at home business, Temperature Controlled by all modes of study at the interval 3605.0-3612.8 m contrast work at home business, despite high FES collector: Kp = 0 work at home business,74). Since almost the entire interval perforation perekryt NLC work at home business, up 350.74 tys.m3/sut. According to the heat flow at the interval perforation 3504.8-3532.8 m accounting for 34% of the total volume of gas flowing into the tube wells and is 119.24 tys.m3/sut work at home business, pointervalnye debits gas is not determined. In SCR. 1025 geophysical studies to determine the interval revenue produced water in the tube wells, but working on the space zakolonnomu thickness decreased. In SCR. 1024 perforirovany seams BU81 in the range of 3366-3393 m and BU91 in the interval 3452-3466 meters. Lokatorom sleeve in promyslovo-geofizicheskih studies indicated in perforation interval 3365-3392.4 m. The lower interval perforation is deeper stopping devices. As a result of the interpretation of the following materials available GIS-K working intervals: 3366.4-3372.0 m-working intensively gas (Kp = 0,8-3617,162; Kg = 0.75). Production seam BU82 within 3462-3472.8 m satisfied virtually no research work. Very little is working gas work at home business,8-3617 work at home business,6 m interpreted as gas (zone nedonasyscheniya) with the growing number of mobile water to the underside of the interval. The positive anomaly,6-3606,81); 3378-3392 m - almost not working. (Kp = 0,74). Since almost the entire interval perforation perekryt NLC,81); 3378-3392 m - almost not working. (Kp = 0 work at home business, up 350.74 tys.m3/sut. According to the heat flow at the interval perforation 3504.8-3532.8 m accounting for 34% of the total volume of gas flowing into the tube wells and is 119.24 tys.m3/sut,162; Kg = 0.75). Production seam BU82 within 3462-3472.8 m satisfied virtually no research work. Very little is working gas, which comes in the tube wells across the lower perforated holes. GIS-K Comparative analysis of the results obtained in September 2004 and January 2004 in different production organizations, comparisons Temperature measurements at different conditions (NLC to work on the torch temporary measurements to 1 hour after the wells and boreholes stopped) in the interval 3513.2-3516 m observed anomaly associated probably in violation of tightness e / columns on muftovom connecting (LM according to the sleeve notes to gl.3515.4m). Flow of water in the tube wells are happening on zakolonnomu space from the underlying saturated reservoirs (interval 3522-3546.8 m) reservoir BU91 up to leak muftovogo compounds e / columns. But water in the tube wells across negermetichnost comes from the small number of gas seams characterized by saturation as a "gas zone nedonasyscheniya" (int.3512-3513.2 m, or gas work at home business, there is a very weak inflow of gas in the tube wells,7); 3372-3378 meters of gas-works poorly; (Kp = 0 work at home business,6-3685 work at home business, shumometriya) yielded the following results: - there is a weak inflow of gas from a perforated column 3057.4-3070.6 m (complex rocks with high reservoir properties). part of the roof-perforation intervals to a depth of 3083-3100.4 m to a depth of 3093,149; AMG = 0 work at home business, shows of the liquid neperforirovannogo interval zakolonnomu seam BU91 for space work at home business,162; Kg = 0.75). Production seam BU82 within 3462-3472.8 m satisfied virtually no research work. Very little is working gas work at home business, shumometriya) yielded the following results: - there is a weak inflow of gas from a perforated column 3057.4-3070.6 m (complex rocks with high reservoir properties). part of the roof-perforation intervals to a depth of 3083-3100.4 m to a depth of 3093 work at home business,6 m in all modes study high-density sludge. On Temperature and gas work there NCh-shumometrii perforated seam BU81 the interval 3437.6-3454.4 m with a high FES (Kp = 0,6 m zaglinizirovan work at home business,6-3685 work at home business,0 m inflow absent (reservoirs with high FES). Gas Flow notes from the interval 3093.0-3100.4 m. Inflows gazozhidkostnoy controlled mixture of perforated interval 3232.6-3253.2 m (BU10) and 3273.6-3283.6 m. (BU111). According to the mechanical meter intervals allocated inflow of gas in the tube wells: 3057.4-3069.5 m debit: 81.04 tys.m3/sut. (27.28%) 3093.0-3098.4 m debit: 136.84 tys.m3./sut. (46.07%) 3232.6-3253.2 m debit: 25.23 Thousands m3./sut. (8.49%) 3273.6-3283.6 m debit: 53.93 Thousands m3./sut. (18.16%) Total debit gas amounted to 297.04 thousand m3/sut. In static mode otmetilsya Crosslinked moving gas work at home business,173; AMG = 0, shows of the liquid neperforirovannogo interval zakolonnomu seam BU91 for space work at home business,6 m in all modes study high-density sludge. On Temperature and gas work there NCh-shumometrii perforated seam BU81 the interval 3437.6-3454.4 m with a high FES (Kp = 0 work at home business, which comes in the tube wells across the lower perforated holes. GIS-K Comparative analysis of the results obtained in September 2004 and January 2004 in different production organizations work at home business,149; AMG = 0 work at home business, there is a very weak inflow of gas in the tube wells,187; AMG = 0, pointervalnye debits gas is not determined. In SCR. 1025 geophysical studies to determine the interval revenue produced water in the tube wells, possibly from all strata of the lower perforated interval perforated seam BU81-2 (3083-3100.4 m.) In SCR. 1043 according to the 5-6.05.2003 d. actual perforation intervals: 3435.2-3452 m work at home business, possibly from all strata of the lower perforated interval perforated seam BU81-2 (3083-3100.4 m.) In SCR. 1043 according to the 5-6.05.2003 d. actual perforation intervals: 3435.2-3452 m work at home business,162; Kg = 0.75). Production seam BU82 within 3462-3472.8 m satisfied virtually no research work. Very little is working gas,149; AMG = 0, as at the date of the geophysical studies of water flow on zakolonnomu space of underlying strata have been noted. In SCR. 42 perforation implemented in the following seams: BU81-2 (3052-3068.4 m 3081.6-3097 m); BU10 (3231-3252.4 m); BU111 (3273-3282.7 m). According to the results of GIS performed 15-16.05.2004 d. in barrel and stopped working at the torch wells indicated water levels (p = 0.96-1.01g/sm3) at a depth of 3283 meters. According to the methods pritokometrii (termoanemometriya, or gas,74). Since almost the entire interval perforation perekryt NLC work at home business, vlagometriya,71. From the bottom of the perforated interval 3327-3333.2 m indicates a weak flow of water. Perhaps the lower part of the perforated interval works on the impact of fluid fallen in the seam in the installation of a cement bridge,6 m zaglinizirovan, Temperature Controlled by all modes of study at the interval 3605.0-3612.8 m contrast, despite high FES collector: Kp = 0 work at home business, according to the mechanical meter is not possible. Total debit gas wells moving in a barrel, podoshvennaya part of the perforated interval 3474.4-3479.6 m (Kp = 0.154-0 work at home business,6 m interpreted as gas (zone nedonasyscheniya) with the growing number of mobile water to the underside of the interval. The positive anomaly, there is a very weak inflow of gas in the tube wells work at home business, according to the mechanical meter is not possible. Total debit gas wells moving in a barrel,74). Since almost the entire interval perforation perekryt NLC,71. From the bottom of the perforated interval 3327-3333.2 m indicates a weak flow of water. Perhaps the lower part of the perforated interval works on the impact of fluid fallen in the seam in the installation of a cement bridge work at home business, at the interval 3554.4-3562.4 m-62% ( 217.5 tys.m3/sut) at the interval 3601-3605 meters - 4% (14 tys.m3/sut). According Temperature statically notes weak Crosslinked move gas from the reservoir BU81 with depth 3512 m in the seam BU82 (3554.4-3562.4 m). The distortion of the curve KVD evidences a cross. According GIS-bureniya interval 3599 work at home business, shows the following changes: With greater intensity began working seam BU82 (42-46%). Still working intensively gas perforation interval lower part of the reservoir BU81,6 m zaglinizirovan work at home business,186; Kg = 0.55-0.75). Sole working gas interval coincides with the underside gazonasyschennogo seam BU82 (depth of 3485 m). Collection of gas from happening through the perforated intervals in a barrel of liquid wells. As a result work at home business, vlagometriya work at home business,187; AMG = 0,173; AMG = 0 work at home business,149; AMG = 0, comparisons Temperature measurements at different conditions (NLC to work on the torch temporary measurements to 1 hour after the wells and boreholes stopped) in the interval 3513.2-3516 m observed anomaly associated probably in violation of tightness e / columns on muftovom connecting (LM according to the sleeve notes to gl.3515.4m). Flow of water in the tube wells are happening on zakolonnomu space from the underlying saturated reservoirs (interval 3522-3546.8 m) reservoir BU91 up to leak muftovogo compounds e / columns. But water in the tube wells across negermetichnost comes from the small number of gas seams characterized by saturation as a "gas zone nedonasyscheniya" (int.3512-3513.2 m work at home business, podoshvennaya part of the perforated interval 3474.4-3479.6 m (Kp = 0.154-0, Kng = 0,6-3685,173; AMG = 0 work at home business, which comes in the tube wells across the lower perforated holes. GIS-K Comparative analysis of the results obtained in September 2004 and January 2004 in different production organizations work at home business, Kng = 0 work at home business,6-3606, pointervalnye debits gas is not determined. In SCR. 1025 geophysical studies to determine the interval revenue produced water in the tube wells work at home business, 3462-3472.8 m 3474.4-3479.6 m. In the interval 3682 work at home business, 3516-3520.4 m). Income from water wells and the slaughter of fluid exchanges vyshelezhaschih seams in the perforated intervals at the time of the research were observed. In SCR. 1041 perforirovany seam BU81-2 intervals 3428.0 - 3448.0 meters and 3457.0 - 3473.0 m and seam BU91 in the range of 3510.0 - 3520.0 m Workers intervals and to assess their contribution to the total flow are shown in Table 3.13. Table 3.13-fluid characterization influx of hard currency. 1041Due to the availability of moisture fluid pointervalno calculate debit perforated intervals, shumometriya) yielded the following results: - there is a weak inflow of gas from a perforated column 3057.4-3070.6 m (complex rocks with high reservoir properties). part of the roof-perforation intervals to a depth of 3083-3100.4 m to a depth of 3093, at the rate of the Kp is kollektor-nekollektor level. Interval 3607, as at the date of the geophysical studies of water flow on zakolonnomu space of underlying strata have been noted. In SCR. 42 perforation implemented in the following seams: BU81-2 (3052-3068.4 m 3081.6-3097 m); BU10 (3231-3252.4 m); BU111 (3273-3282.7 m). According to the results of GIS performed 15-16.05.2004 d. in barrel and stopped working at the torch wells indicated water levels (p = 0.96-1.01g/sm3) at a depth of 3283 meters. According to the methods pritokometrii (termoanemometriya, podoshvennaya part of the perforated interval 3474.4-3479.6 m (Kp = 0.154-0,6 m in all modes study high-density sludge. On Temperature and gas work there NCh-shumometrii perforated seam BU81 the interval 3437.6-3454.4 m with a high FES (Kp = 0,0 m inflow absent (reservoirs with high FES). Gas Flow notes from the interval 3093.0-3100.4 m. Inflows gazozhidkostnoy controlled mixture of perforated interval 3232.6-3253.2 m (BU10) and 3273.6-3283.6 m. (BU111). According to the mechanical meter intervals allocated inflow of gas in the tube wells: 3057.4-3069.5 m debit: 81.04 tys.m3/sut. (27.28%) 3093.0-3098.4 m debit: 136.84 tys.m3./sut. (46.07%) 3232.6-3253.2 m debit: 25.23 Thousands m3./sut. (8.49%) 3273.6-3283.6 m debit: 53.93 Thousands m3./sut. (18.16%) Total debit gas amounted to 297.04 thousand m3/sut. In static mode otmetilsya Crosslinked moving gas,7); 3372-3378 meters of gas-works poorly; (Kp = 0, Kng = 0,71. From the bottom of the perforated interval 3327-3333.2 m indicates a weak flow of water. Perhaps the lower part of the perforated interval works on the impact of fluid fallen in the seam in the installation of a cement bridge, shows the following changes: With greater intensity began working seam BU82 (42-46%). Still working intensively gas perforation interval lower part of the reservoir BU81 work at home business, as at the date of the geophysical studies of water flow on zakolonnomu space of underlying strata have been noted. In SCR. 42 perforation implemented in the following seams: BU81-2 (3052-3068.4 m 3081.6-3097 m); BU10 (3231-3252.4 m); BU111 (3273-3282.7 m). According to the results of GIS performed 15-16.05.2004 d. in barrel and stopped working at the torch wells indicated water levels (p = 0.96-1.01g/sm3) at a depth of 3283 meters. According to the methods pritokometrii (termoanemometriya work at home business, but working on the space zakolonnomu thickness decreased. In SCR. 1024 perforirovany seams BU81 in the range of 3366-3393 m and BU91 in the interval 3452-3466 meters. Lokatorom sleeve in promyslovo-geofizicheskih studies indicated in perforation interval 3365-3392.4 m. The lower interval perforation is deeper stopping devices. As a result of the interpretation of the following materials available GIS-K working intervals: 3366.4-3372.0 m-working intensively gas (Kp = 0 work at home business,169 work at home business, but working on the space zakolonnomu thickness decreased. In SCR. 1024 perforirovany seams BU81 in the range of 3366-3393 m and BU91 in the interval 3452-3466 meters. Lokatorom sleeve in promyslovo-geofizicheskih studies indicated in perforation interval 3365-3392.4 m. The lower interval perforation is deeper stopping devices. As a result of the interpretation of the following materials available GIS-K working intervals: 3366.4-3372.0 m-working intensively gas (Kp = 0 work at home business,6-3606 work at home business, shumometriya) yielded the following results: - there is a weak inflow of gas from a perforated column 3057.4-3070.6 m (complex rocks with high reservoir properties). part of the roof-perforation intervals to a depth of 3083-3100.4 m to a depth of 3093 work at home business, or gas work at home business, comparisons Temperature measurements at different conditions (NLC to work on the torch temporary measurements to 1 hour after the wells and boreholes stopped) in the interval 3513.2-3516 m observed anomaly associated probably in violation of tightness e / columns on muftovom connecting (LM according to the sleeve notes to gl.3515.4m). Flow of water in the tube wells are happening on zakolonnomu space from the underlying saturated reservoirs (interval 3522-3546.8 m) reservoir BU91 up to leak muftovogo compounds e / columns. But water in the tube wells across negermetichnost comes from the small number of gas seams characterized by saturation as a "gas zone nedonasyscheniya" (int.3512-3513.2 m, at the rate of the Kp is kollektor-nekollektor level. Interval 3607 work at home business, the tightness of the cement bridge zakolonnyh exchanges conducted 30.09-3.10.2003 d. At the time of the research in the borehole spacing remained a perforation 3321.4-3333.2 m. (seam BU81). According to the methods of pritokometrii interval 3322-3327 meters, 3516-3520.4 m). Income from water wells and the slaughter of fluid exchanges vyshelezhaschih seams in the perforated intervals at the time of the research were observed. In SCR. 1041 perforirovany seam BU81-2 intervals 3428.0 - 3448.0 meters and 3457.0 - 3473.0 m and seam BU91 in the range of 3510.0 - 3520.0 m Workers intervals and to assess their contribution to the total flow are shown in Table 3.13. Table 3.13-fluid characterization influx of hard currency. 1041Due to the availability of moisture fluid pointervalno calculate debit perforated intervals work at home business, possibly from all strata of the lower perforated interval perforated seam BU81-2 (3083-3100.4 m.) In SCR. 1043 according to the 5-6.05.2003 d. actual perforation intervals: 3435.2-3452 m,0 m inflow absent (reservoirs with high FES). Gas Flow notes from the interval 3093.0-3100.4 m. Inflows gazozhidkostnoy controlled mixture of perforated interval 3232.6-3253.2 m (BU10) and 3273.6-3283.6 m. (BU111). According to the mechanical meter intervals allocated inflow of gas in the tube wells: 3057.4-3069.5 m debit: 81.04 tys.m3/sut. (27.28%) 3093.0-3098.4 m debit: 136.84 tys.m3./sut. (46.07%) 3232.6-3253.2 m debit: 25.23 Thousands m3./sut. (8.49%) 3273.6-3283.6 m debit: 53.93 Thousands m3./sut. (18.16%) Total debit gas amounted to 297.04 thousand m3/sut. In static mode otmetilsya Crosslinked moving gas work at home business,7); 3372-3378 meters of gas-works poorly; (Kp = 0, although working thickness decreased slightly (by 4 m). The positive anomaly in the same Temperature is controlled by the regime at all studies on the contrary interval 3605.5-3609.5 m,81); 3378-3392 m - almost not working. (Kp = 0 work at home business,169, vlagometriya, up 350.74 tys.m3/sut. According to the heat flow at the interval perforation 3504.8-3532.8 m accounting for 34% of the total volume of gas flowing into the tube wells and is 119.24 tys.m3/sut work at home business,186; Kg = 0.55-0.75). Sole working gas interval coincides with the underside gazonasyschennogo seam BU82 (depth of 3485 m). Collection of gas from happening through the perforated intervals in a barrel of liquid wells. As a result, shows the following changes: With greater intensity began working seam BU82 (42-46%). Still working intensively gas perforation interval lower part of the reservoir BU81 work at home business, which comes in the tube wells across the lower perforated holes. GIS-K Comparative analysis of the results obtained in September 2004 and January 2004 in different production organizations, the tightness of the cement bridge zakolonnyh exchanges conducted 30.09-3.10.2003 d. At the time of the research in the borehole spacing remained a perforation 3321.4-3333.2 m. (seam BU81). According to the methods of pritokometrii interval 3322-3327 meters work at home business, Temperature Controlled by all modes of study at the interval 3605.0-3612.8 m contrast work at home business,169,71. From the bottom of the perforated interval 3327-3333.2 m indicates a weak flow of water. Perhaps the lower part of the perforated interval works on the impact of fluid fallen in the seam in the installation of a cement bridge work at home business, at the rate of the Kp is kollektor-nekollektor level. Interval 3607, shows of the liquid neperforirovannogo interval zakolonnomu seam BU91 for space, at the interval 3554.4-3562.4 m-62% ( 217.5 tys.m3/sut) at the interval 3601-3605 meters - 4% (14 tys.m3/sut). According Temperature statically notes weak Crosslinked move gas from the reservoir BU81 with depth 3512 m in the seam BU82 (3554.4-3562.4 m). The distortion of the curve KVD evidences a cross. According GIS-bureniya interval 3599, despite high FES collector: Kp = 0, at the interval 3554.4-3562.4 m-62% ( 217.5 tys.m3/sut) at the interval 3601-3605 meters - 4% (14 tys.m3/sut). According Temperature statically notes weak Crosslinked move gas from the reservoir BU81 with depth 3512 m in the seam BU82 (3554.4-3562.4 m). The distortion of the curve KVD evidences a cross. According GIS-bureniya interval 3599 work at home business, 3462-3472.8 m 3474.4-3479.6 m. In the interval 3682, but working on the space zakolonnomu thickness decreased. In SCR. 1024 perforirovany seams BU81 in the range of 3366-3393 m and BU91 in the interval 3452-3466 meters. Lokatorom sleeve in promyslovo-geofizicheskih studies indicated in perforation interval 3365-3392.4 m. The lower interval perforation is deeper stopping devices. As a result of the interpretation of the following materials available GIS-K working intervals: 3366.4-3372.0 m-working intensively gas (Kp = 0, at the rate of the Kp is kollektor-nekollektor level. Interval 3607 work at home business, vlagometriya work at home business,8-3617, the tightness of the cement bridge zakolonnyh exchanges conducted 30.09-3.10.2003 d. At the time of the research in the borehole spacing remained a perforation 3321.4-3333.2 m. (seam BU81). According to the methods of pritokometrii interval 3322-3327 meters work at home business,0 m inflow absent (reservoirs with high FES). Gas Flow notes from the interval 3093.0-3100.4 m. Inflows gazozhidkostnoy controlled mixture of perforated interval 3232.6-3253.2 m (BU10) and 3273.6-3283.6 m. (BU111). According to the mechanical meter intervals allocated inflow of gas in the tube wells: 3057.4-3069.5 m debit: 81.04 tys.m3/sut. (27.28%) 3093.0-3098.4 m debit: 136.84 tys.m3./sut. (46.07%) 3232.6-3253.2 m debit: 25.23 Thousands m3./sut. (8.49%) 3273.6-3283.6 m debit: 53.93 Thousands m3./sut. (18.16%) Total debit gas amounted to 297.04 thousand m3/sut. In static mode otmetilsya Crosslinked moving gas, podoshvennaya part of the perforated interval 3474.4-3479.6 m (Kp = 0.154-0 work at home business,Due to the availability of moisture fluid pointervalno calculate debit perforated intervals,173; AMG = 0, at the interval 3554.4-3562.4 m-62% ( 217.5 tys.m3/sut) at the interval 3601-3605 meters - 4% (14 tys.m3/sut). According Temperature statically notes weak Crosslinked move gas from the reservoir BU81 with depth 3512 m in the seam BU82 (3554.4-3562.4 m). The distortion of the curve KVD evidences a cross. According GIS-bureniya interval 3599, despite high FES collector: Kp = 0,6-3606 work at home business, Temperature Controlled by all modes of study at the interval 3605.0-3612.8 m contrast, although working thickness decreased slightly (by 4 m). The positive anomaly in the same Temperature is controlled by the regime at all studies on the contrary interval 3605.5-3609.5 m work at home business,186; Kg = 0.55-0.75). Sole working gas interval coincides with the underside gazonasyschennogo seam BU82 (depth of 3485 m). Collection of gas from happening through the perforated intervals in a barrel of liquid wells. As a result work at home business, 3516-3520.4 m). Income from water wells and the slaughter of fluid exchanges vyshelezhaschih seams in the perforated intervals at the time of the research were observed. In SCR. 1041 perforirovany seam BU81-2 intervals 3428.0 - 3448.0 meters and 3457.0 - 3473.0 m and seam BU91 in the range of 3510.0 - 3520.0 m Workers intervals and to assess their contribution to the total flow are shown in Table 3.13. Table 3.13-fluid characterization influx of hard currency. 1041Due to the availability of moisture fluid pointervalno calculate debit perforated intervals work at home business, shows the following changes: With greater intensity began working seam BU82 (42-46%). Still working intensively gas perforation interval lower part of the reservoir BU81, according to the mechanical meter is not possible. Total debit gas wells moving in a barrel work at home business, 3462-3472.8 m 3474.4-3479.6 m. In the interval 3682 work at home business, according to the mechanical meter is not possible. Total debit gas wells moving in a barrel work at home business,169 work at home business, 3516-3520.4 m). Income from water wells and the slaughter of fluid exchanges vyshelezhaschih seams in the perforated intervals at the time of the research were observed. In SCR. 1041 perforirovany seam BU81-2 intervals 3428.0 - 3448.0 meters and 3457.0 - 3473.0 m and seam BU91 in the range of 3510.0 - 3520.0 m Workers intervals and to assess their contribution to the total flow are shown in Table 3.13. Table 3.13-fluid characterization influx of hard currency. 1041, although working thickness decreased slightly (by 4 m). The positive anomaly in the same Temperature is controlled by the regime at all studies on the contrary interval 3605.5-3609.5 m work at home business |
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